探究混凝-溶气气浮-过滤工艺在污水深度处理方面的可行性。以武汉市某污水处理厂A2O工艺二沉池出水为原水,进行了混凝-溶气气浮-过滤深度处理工艺中试研究。试验完成了回流比、加药量、表面负荷三个主要影响因素的三因素三水平正交实验,以COD、总磷、浊度去除率为考察指标,结果表明:加药量对COD、总磷、浊度去除效果影响均最为显著,推荐工艺最佳运行参数为表面负荷11.11m3/m2?h,加药量10mg/L,回流比12%,且在此运行条件下,单位水处理电耗与药耗总共为0.039元/m3;同时在固定表面负荷10m3/m2?h条件下进行了连续流实验,结果表明:在一定水质波动条件下,该工艺连续运行可靠、处理效果稳定,出水COD浓度稳定低于15mg/L、出水总磷浓度稳定低于0.1mg/L,出水浊度低于0.5NTU,有一定工程应用前景。
Abstract
To explore the feasibility of the coagulation-dissolved air flotation(DAF)-filtration process in the advanced wastewater treatment, a pilot study on the coagulation- dissolved air flotation-filtration advanced treatment process was carried out in a sewage treatment plant of Wuhan with the effluent from the secondary sedimentation tank of A2O process as raw water. The experiment completed the three factors and three levels orthogonal experiment of reflux ratio、dosage of coagulant、surface load three factors, COD、TP、turbidity removal rate as the evaluation index, the results showed that the dosage had the most significant effect on the removal of COD, total phosphorus and turbidity. The optimum operating parameters of the recommended process were surface load of 11.11m3/m2?h, dosage of 10mg/L and reflux ratio of 12%. Under this operating conditions, the unit water treatment power consumption and drug consumption for a total of 0.039yuan/m3; At the same time, the continuous flow test was carried out under the condition of fixed surface load of 10m3/m2?h. The results showed that under a certain water quality fluctuation condition, the process was reliable, the treatment effect was stable, the effluent COD concentration was stable below 15mg/L, The concentration is stable below 0.1mg/L, the turbidity of the effluent is less than 0.5 NTU, which has certain engineering application prospect.
关键词
混凝 /
气浮 /
过滤 /
污水深度处理
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Key words
Coagulation /
Dissolved air flotation (DAF) /
Filtration /
Advanced wastewater treatmen
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